The main reason for mentioning this seemingly simple operation is to tell you a problem that occurs when a piece like this is clamped from it's internal diameter. As the piece is machined it heats up and expands, this causes it to come loose on the chuck. There are probably more sophisticated techniques for dealing with this but I simply kept tightening the chuck between operations and when it started making noise. I expect that flooding the work with coolant would also have worked. I'd be interested to know if anyone has any other solutions to this issue.
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